http://repository.iitr.ac.in/handle/123456789/2448
DC Field | Value | Language |
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dc.contributor.author | Chauhan S.S. | - |
dc.contributor.author | Khanam, Shabina | - |
dc.date.accessioned | 2020-10-06T14:09:38Z | - |
dc.date.available | 2020-10-06T14:09:38Z | - |
dc.date.issued | 2019 | - |
dc.identifier.citation | Energy (2019), 173(): 364-373 | - |
dc.identifier.issn | 3605442 | - |
dc.identifier.uri | https://doi.org/10.1016/j.energy.2019.02.084 | - |
dc.identifier.uri | http://repository.iitr.ac.in/handle/123456789/2448 | - |
dc.description.abstract | In this study, pinch analysis is employed to integrate energy in steam cycle of a 250 MW thermal power plant (TPP) located in Rajasthan state of India. To apply pinch analysis on steam turbine, all extractions exiting the turbine are considered as hot utility and feedwater as cold utility. Pinch analysis shows the potential savings in hot and cold utilities as 9.66% and 0.77%, respectively. Considering heat transfer across the pinch in condenser, heat available in boiler blow down and flowrates of extraction of low pressure (LP) turbine, six different energy integration schemes are proposed. Results show that extraction of LP turbine entering to LPH-1 is eliminated, which saves steam extracted from turbine for preheating the feedwater and thus, extra power is generated. It is also seen that flowrates from other two extractions of LP turbine decrease marginally. Amongst six energy integration schemes, the best one indicates that using pinch analysis, net generated power is increased by 0.55% and demineralized water demand is reduced by 57.6%. Further, exergy analysis of steam cycle is carried out and compared with that of most suited retrofitted scheme. Results of the present study are compared well with that of published literature. © 2019 Elsevier Ltd | - |
dc.language.iso | en_US | - |
dc.publisher | Elsevier Ltd | - |
dc.relation.ispartof | Energy | - |
dc.subject | Boiler blowdown | - |
dc.subject | Energy integration | - |
dc.subject | Exergy analysis | - |
dc.subject | LP turbine | - |
dc.subject | Steam cycle | - |
dc.subject | Thermal power plant | - |
dc.title | Enhancement of efficiency for steam cycle of thermal power plants using process integration | - |
dc.type | Article | - |
dc.scopusid | 36136502800 | - |
dc.scopusid | 23025264900 | - |
dc.affiliation | Chauhan, S.S., Department of Chemical Engineering, Indian Institute of Technology Roorkee, Roorkee, 247 667, India | - |
dc.affiliation | Khanam, S., Department of Chemical Engineering, Indian Institute of Technology Roorkee, Roorkee, 247 667, India | - |
dc.description.correspondingauthor | Chauhan, S.S.; Department of Chemical Engineering, Indian Institute of Technology RoorkeeIndia; email: chauhaniet04@gmail.com | - |
Appears in Collections: | Journal Publications [CH] |
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